Sunday, March 29, 2020

New uses for propane cook stove

Had another go at heating the cases. Took the old propane camp stove and added "C" clamps to hold the case off the flame.  The first try, even with the water splatter method the bearing race stuck in and failed to drop the whole distance. Ok, reheated it and tapped the race back out.  Gave it some time to cool the whole lot down before another go.

On the second go around I used a pyrometer attachment to the DVOM.  When it got to about 288`f or so I grabbed the race and gave it a try. CLINK with a drop right in. Well ok then, this is moving in the right direction. After letting it cool about an hour I brought it back in for measurements. 

Sunday, March 22, 2020

Velocette MSS shim battles continues

So I had at it and used the Roger Welsch; heat- beat- repeat technique.  The verdict?- no love. The main race just would not budge. The first set was using a heat gun; now this works on BMW gear boxes almost all of the time.  But then again , this is no BMW.  so after three  tries I moved onto a puller with heat. The object was to minimize damage if any.  Still no love.  

At this point I took a few hour break before I did (break something!).  And back at it with heat and beat. still no love. So I setup the press and tried with more heat. Nope, not a hit of movement.  Now I'm sure that there are a few of you out there that would have a better approach. This is what I had today and now.  

My concerns were not to heat it so much to warp the case but the heat gun was not working.  On to Propane.  It did get things moving faster, but still no love.  set it cool for a bit and get back into it later in the day.  an hour later, heat the spice out of it...      and there we has just a slight movement. then stop.  More heat, more beat.  some little improvements but this is taking WAAYYYY longer than needs be. I think of the old chap that broke his bike at the club race on Saturday and needs this for Monday morning. Looks like I'll be walking to work tomorrow. 
  After what seemed to be an eternity the race came out along with a set of destroyed brass shims.

After a conference over Marconi and Bell to those in the know it seems that there still was not enough heat. And I was ready to machine up a spacer for a drift to tap the race back in. 

Well at this point the game is to play with heat, to see how much heat it takes for the race to drop in.  And then reverse the process to make it drop back out.  Once we get to that level-we'll give it a shimming.  The golden turn around. 

Saturday, March 21, 2020

Velocette Crankshaft endplay testing, maybe?

After a few months of procrastinating on the old MSS engine, it was time to get the next step going on it.As simple as this job seems to be, it has taken me months to figure out the approach.  This is even after watching the Velocette Owners Club engine overhaul video by Dave Allcock.  Even then I could be doing this all wrong but here it goes.

The simple process; place the crankshaft back into the case halves.  Space the two case halves apart with 0.004 shim stock and measure out the end play. Any end play found is the needed shim at the main bearing race.  The crankshaft should have 0.004 nip up or preload.  Sounded simple enough... But what if there is no end play when you measure it?

So the hold up have been the jigging up for measuring end play.  All the while, something in the video didn't quite make sense. The concept was right but the measuring seemed strange.  If you use the 0.004" shims and your looking to make 0.004" nip up wouldn't that measure out to 0.0?  Now, obviously if you are starting without any shims under the main bearings all is fine. But what if your testing an engine that has already been shimmed?

Well, I don't have any convenient 0.004" shim stock. I do however have 0.006". And maybe this is where things could be going wrong. The thought was that 0.006" shim stock would mean that if the cases are nipped up and your looking for 0.004" , with a 0.006" you'd have 0.002" play as you lifted the cases while the drive side of the crankshaft was locked into a vise.  The dial gauge would be affixed to the case in some fashion.

This was the mucking about that has taken months to get down to. Gathering bolts, cutting and filing the shims. Then making a simple bracket to allow the magnetic base of the dial attach to. In the club video it looks at if Dave attaches the dial indicator to the vise then takes the measurement from the case. The current vise in my workshop doesn't seem to be long enough to do as such. So will attaching the dial indicator to the case and measure the crank work? Dave also uses 0.004" shim stock to take the place of the nip up.

Set at rest
heavy lifting on case
 So where are we? Dunno, but this all makes me think that the shimming is too tight. On to removing the shim and try again. While were at it, the reason for this journey is due to the fact that when I got this engine it had been sitting for many years in a basement. When it was pulled apart, the cylinder was all worn  out and there was no piston. In between the cases was a cork gasket and from what the books show is that there is no cork gasket sealing the two case halves. Which begs the question, was it shimmed properly or was it shimmed for cork gaskets...  nothings ever easy.
The last step was to heat up the case half, remove the bearing race, check the shim. Then reinstall the race sans shim and do it all over again. If we get 0.002" play at the dial indicator ~ happy day, if not, back to the drawing board.

After about an hour a thought occurred to me, that if .006" shim stock gives no to little play why not try thicker shim stock as re-check for play? ok, back at it